I worked on the Mustang today repairing and getting my heating and defrosting system back up and running. So why go through this? Car is a street rod and I only ride during the summer season. WRONG! I can go without a heater for warmth but driving at night at near freezing temps and fog your windshield is constantly getting condensation even with the windows rolled down. I had to drive 2 hours like that using a towel to wipe a spot clean every so often and this is coming down from the mountains on twisted 2 way lanes.
Thought it would be a cheap reassurance the next time the situation popped up. Parts were cheap the labor is what took me so long. I estimate over four hours of work, mostly because I’m so big it’s hard to get under the passenger dashboard area. Luckily it’s not the driver side with the steering wheel in the way.
The original heater core was definitely leaking so it was a good call to just get a replacement. Looking at the aluminum heater core I’m guessing it was replaced before. The original cores back then I believe were made from brass.
After driving around the mustang for a couple months without power steering or power brakes I decided it was enough. I was lucky to locate a Craigslist seller that had all the power parts I needed from a 1970 Mach 1 model. This would almost be a drop in upgrade. A few misc parts would have to be fabricated. In my case the master cylinder brake lines to distribution block and a major part was the custom billet power steering pump which I could not find already made. My buddy had to CNC the part after he designed it, not a trivial task.
All the parts that I bought worked! I don’t even have any leaks from any of the parts that purchased.
One the attention to detail mods used a braided steel hosing for a vacuum function. This is way overkill for the application but looks really good coming from the rear of the intake manifold into the power booster.
The aftermarket style oil dipstick was relocated from bolting to the front of the intake manifold to a section in between the alternator bracket spacer location. This gave it a straight shot without bending the tubular guide.
I’ve been working on the man cave for some time now. I’ve always like the look of a clean functional garage that was fun to work in, have all the necessary tools and a good entertainment setup. The garage is a decent size area but I have have too many toys in it so it looks really cluttered.
The drivers side door trim was in really bad shape. The rear section was held down using a visible screw. I was able find a replacement piece on fleaBay for a very low price. Once I figured out how to properly install the plastic fasteners it was an easy installation.
I finally made arrangements to get rid of the Direct TV services and switch over to Xfinity. I used to have their service many years ago but unsubscribed when they kept increasing the monthly cost. I now have both internet and television services from the same provider.
I worked on cleaning the the power steering box tonight. Sucker is filthy. Trying to use engine degreaser and a wire brush to remove most of the crud. I checked the steering “slop” or play as it is sometimes referred to. It seems to be tight and no adjustments necessary.
It may not even be necessary to do all the cleaning since the steering box will be hidden below.
I pulled the coupe out for a ride today and it was pulling severely to the right. I pulled over to give it a look and found the right front tire pulled out of the head and no air! I was able to hobble back home and pull the wheel off. I also found that I have a security bolt on each wheel. Luckily I noticed that the security bolt key was in my glove box. I was able to jack the car up and remove the tire.
After inspecting the tire I couldn’t find any indication of an object piercing the tire so I took it over to the Pepboyz auto center. They performed three dunk test and searched for bubbles indicating a hole. None to be found. It’s possible that the bead dislodged during a severe hit of some sort and slowly loss air. I will check the other front tire for proper air pressure.
I need to keep an on this as I ride around without a spare tire. I always figured I’d just get the car towed home if it was disabled or had a flat tire.
I have most of the parts to do a full power brake and power steering upgrade this winter. After trying a mock up run I discovered the bolts were not even the same. The power steering bracket from the 351 Cleveland is 5/8″ and the 302 head bolts for mounting 9/16″. I’m going to have custom brackets made and the bolts fit properly into the head.
I’ll have to clean up the steering box before doing the installation. I checked the play between the rat joint and the pitman arm and there is no discernible movement. I was planning on adjusting it but it’s not necessary. I think I will try brake cleaner or the engine degreaser in a can that’s available at the local auto part store.
I’m totally impressed with the Prius and the gas mileage it has been getting. I’m getting about 50.5 miles on a gallon of 87 octane gas. That’s very impressive and helpful since the there has been a recent gas tax increase.
I’ve been using the ECO mode exclusively. I tried using the power mode but it’s not necessary in the flat lands I commute in daily.